ACS800 Tripping sometimes at the startup. Fault is 2310. Over current
Drive is configured for winder application and operation thru Profibus DP. Torque control macro and DTC used for it. sometimes when the run command received drive torque is going to negative for a while and the drive is being tripped with over current fault. which is happening within few milliseconds after receiving the run command.
I figured out abvoe point by set the drive speed feedback as internal instead of encoder (bypassed the encoder feedback).
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